KILOWATTS FROM CORNOBS
(Page 3 of 6)
In effect, this not only reduces temperature variations
within the combustion chamber, but also expands
that zone to provide an increase in gas production without
enlarging the 16" hearth diameter. (The design has, after
100 hours of running time, shown no slag buildup, minimal
start-up times, and consist ent temperature levels, while
still being stonesimple. In all fairness, though, a
constantspeed powerplant, such as the type used with this
generator, places relatively few requisites upon a gasifier
... because of the fact that gas demand doesn't ever
fluctuate with varying engine speeds.)
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The hearth's size, configuration, and composition were
based upon the nature of the fuel and the cost of the
hearth. Although historical data indicated that a specific
hearth diameter was necessary to supply a given size of
engine, and that a restriction within the chamber was
desirable to maintain sufficient temperatures, Haug
successfully used a 16"-diameter straight steel pipe, and
merely installed a movable grate inside it to serve as a
shaker. Because there appeared to be no need to "funnel
down" the flow of gases, there was no reason to cast the
hearth into a special shape. Thus additional savings were
realized.
By the same token, it was decided-with an eye toward the
eventual commercialization of the technology—not to
try to upscale the unit to suit larger powerplants.
Instead, a modular approach—in which additional
small gasifiers could be added on line as
required-seemed more desirable from both a technical
standpoint (the single hearth for a 1,000-KW plant would
need to be a flow-choking sixfeet in
diameter), and a practical one (parts availability and
interchangeability would be a problem in gargantuan-scale
gasifiers).
Finally, in an effort to determine what the minimum
assembly costs might be, the Odin team experimented with a
variety of metal and PVC cooling mechanisms, wet and dry
filters, and simple moisture traps ... all of which would
serve to prepare the gaseous fuel prior to delivery to
their 35-KW diesel generator. The best results were
realized by using steel cooling towers housed in water
jackets ... installing flat-nipple, vacuum-operated diesel
truck water traps in the gas pipe ... and mounting a dry
cyclone filter—followed by a percolating oil-bath
chamber—in the line directly before the Detroit
diesel generator's air inlet.
Since the standby powerplant used in their research wasn't
equipped with a dual-fuel system, the Odin folks had to
make do by merely introducing fuel gas into the engine's
airstream. Unfortunately, the design of their particular
powerplant didn't lend itself a full range of pilot fuel
adjustment, so they, could only operate on a maximum of 80
corn gas. (Norwegian studies indicate that 24 little as 8%
diesel pilot fuel can be used when the injection is
properly adjusted, and that only a 20% sacrifice in output,
as compared to that when diesel fuel alone is
used, will occur under these conditions.)
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